ISSN 1673-8217 CN 41-1388/TE
Supervisor:China Petrochemical Corporation Limited Sponsor:Sinopec Henan Oilfield Company
2013: Research on using casing pressure to control tubing leakage. Petroleum Geology and Engineering, 27(04): 137-138+141+150.
Citation: 2013: Research on using casing pressure to control tubing leakage. Petroleum Geology and Engineering, 27(04): 137-138+141+150.

Research on using casing pressure to control tubing leakage

  • The liquid volume of A-well on an offshore production platform significantly decreased after it has been put into production.On the wellhead pressure-holding data analysis we conclude that there exists the phenomenon of tubing leakage.Considering the operation cost of the offshore oil wells , we plan to adopt the method of holding casing pressure of oil wells to maintain the high production level of the well. Through the production tests of holding pressure on-site we determine that the casing pressure be controlled at 3.4 MPa can better control leakage , and also can maintain higher submergence depth.At this time wells can normally operate with liquid production of 14.5 t / d.
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