ISSN 1673-8217 CN 41-1388/TE
主管:中国石油化工集团有限公司 主办:中国石油化工股份有限公司河南油田分公司
吴大伟, 吴雪琴, 张容志. 2013: 运用套压控制油管管柱漏失方法研究. 石油地质与工程, 27(04): 137-138+141+150.
引用本文: 吴大伟, 吴雪琴, 张容志. 2013: 运用套压控制油管管柱漏失方法研究. 石油地质与工程, 27(04): 137-138+141+150.
2013: Research on using casing pressure to control tubing leakage. Petroleum Geology and Engineering, 27(04): 137-138+141+150.
Citation: 2013: Research on using casing pressure to control tubing leakage. Petroleum Geology and Engineering, 27(04): 137-138+141+150.

运用套压控制油管管柱漏失方法研究

Research on using casing pressure to control tubing leakage

  • 摘要: 老178块海上生产平台A井投产后液量下降明显,对井口憋压数据分析认为该井存在管柱漏失现象,综合考虑海上油井作业成本,拟采用憋油井套压法维持该井较高水平生产。通过现场憋压生产试验,确定将油井套压控制在3.4MPa时,能较好的控制漏失,且能保持较高沉没度,油井在液量14.5t/d的水平正常进行。

     

    Abstract: The liquid volume of A-well on an offshore production platform significantly decreased after it has been put into production.On the wellhead pressure-holding data analysis we conclude that there exists the phenomenon of tubing leakage.Considering the operation cost of the offshore oil wells , we plan to adopt the method of holding casing pressure of oil wells to maintain the high production level of the well. Through the production tests of holding pressure on-site we determine that the casing pressure be controlled at 3.4 MPa can better control leakage , and also can maintain higher submergence depth.At this time wells can normally operate with liquid production of 14.5 t / d.

     

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